I'm testing a Williamson style input stage with a 6SN7 and the bode plot shows a rolloff of more than 10 dB when the frequency goes up.
Of course I tested the signal generator too and it's flat within 1dB up to 100 kHz.
I measured at the top of the first anode, using a 1 uF capacitor into a 10M probe. The capacitor is there to get only AC for the probe.
The next tube is another 6SN7 with 220K from grid to ground.
What could be wrong? What else should I measure to get a better understanding of what's going on here?
Regards, Gerrit
Of course I tested the signal generator too and it's flat within 1dB up to 100 kHz.
I measured at the top of the first anode, using a 1 uF capacitor into a 10M probe. The capacitor is there to get only AC for the probe.
The next tube is another 6SN7 with 220K from grid to ground.
What could be wrong? What else should I measure to get a better understanding of what's going on here?
Regards, Gerrit
Attachments
Hi Jan,
There is no feedback anywhere in the circuit.
What could cause positive feedback when it's not part an intended part of the circuit.
Regards, Gerrit
There is no feedback anywhere in the circuit.
What could cause positive feedback when it's not part an intended part of the circuit.
Regards, Gerrit
Hi Merlin,
My PSU is a zener regulated MOSFET source follower with approx. 400 VDC output.
I will check tomorrow or perhaps this evening with more decoupling.
As you can see both the input tube and the phase inverter are on the same power rail.
Regards, Gerrit
My PSU is a zener regulated MOSFET source follower with approx. 400 VDC output.
I will check tomorrow or perhaps this evening with more decoupling.
As you can see both the input tube and the phase inverter are on the same power rail.
Regards, Gerrit
I don't know because I only see part of the circuit.Hi Jan,
There is no feedback anywhere in the circuit.
What could cause positive feedback when it's not part an intended part of the circuit.
Regards, Gerrit
Jan
Jan,
There is no feedback into the part of the circuit that is shown.
So how could it be influenced by feedback? I don’t get it right now.
There is no feedback added in the entire circuit.
Regards, Gerrit
There is no feedback into the part of the circuit that is shown.
So how could it be influenced by feedback? I don’t get it right now.
There is no feedback added in the entire circuit.
Regards, Gerrit
Hi Koonw,
I will check this tomorrow.
Could you share your ltSpice file with me? I would like to see how you create the frequency response diagram.
Regards, Gerrit
I will check this tomorrow.
Could you share your ltSpice file with me? I would like to see how you create the frequency response diagram.
Regards, Gerrit
Maybe replace LED1 with an appropriately sized cathode resistor and see if the problem goes away,
I already tried using a single cathode resistor (without the LED); I tried with several values without any difference to the frequency response.
Regards, Gerrit
Regards, Gerrit
I can't view the .asc because I'm not at my computer with LTspice on it, but...
What is the decoupling network from the output stage to this cathodyne stage?
Is there one plate supply feed common to this cathodyne stage and the driven push-pull output stage?
Is this a push-pull power amp? What about the time constants formed by bypass cap(s) on cathode bias resistor(s)?
What is the decoupling network from the output stage to this cathodyne stage?
My PSU is a zener regulated MOSFET source follower with approx. 400 VDC output.
Is there one plate supply feed common to this cathodyne stage and the driven push-pull output stage?
Is this a push-pull power amp? What about the time constants formed by bypass cap(s) on cathode bias resistor(s)?
Maybe make sure R2 is really 1K? Sort of an odd frequency turnover that I would not expect with that schematic.
Looks like the B+ to the first stage has a rather large value of dropping resistor, and lacks enough decoupling
to avoid a boost at lower frequencies. If you run the first stage directly with a lab supply, the boost will go away.
to avoid a boost at lower frequencies. If you run the first stage directly with a lab supply, the boost will go away.
Thanks for all input, this is very much appreciated.
1. R2 is absolutely 1K, but I will measure it again to be 1000% sure.
2. I have a lab supply 0 - 600 VDC @ 2Amp. I will try this too tomorrow (and with extra decoupling).
3. I can try a different anode resistor value, but according to Koonw’s ltSpice simulation this should be OK.
Regards, Gerrit
1. R2 is absolutely 1K, but I will measure it again to be 1000% sure.
2. I have a lab supply 0 - 600 VDC @ 2Amp. I will try this too tomorrow (and with extra decoupling).
3. I can try a different anode resistor value, but according to Koonw’s ltSpice simulation this should be OK.
Regards, Gerrit
Rongon,
The 400 VDC regulated supply is created from my 600+ VDC raw DC voltage. In order to keep the MOSFET in the 400 VDC regulater a bit cooler I use a few high wattage series resistors. They are just getting warm, not hot. The same goes for the MOSFET.
I use another regulated circuit to feed the final tubes with approx. 600 VDC.
Yes, it’s a Push Pull amplifier. The pain however is (only) in the input stage. I don’t measure a significant difference in frequency response between (1) input stage as described in post 1 and (2) the output measured over my 4 Ohm dummy load.
Regards, Gerrit
The 400 VDC regulated supply is created from my 600+ VDC raw DC voltage. In order to keep the MOSFET in the 400 VDC regulater a bit cooler I use a few high wattage series resistors. They are just getting warm, not hot. The same goes for the MOSFET.
I use another regulated circuit to feed the final tubes with approx. 600 VDC.
Yes, it’s a Push Pull amplifier. The pain however is (only) in the input stage. I don’t measure a significant difference in frequency response between (1) input stage as described in post 1 and (2) the output measured over my 4 Ohm dummy load.
Regards, Gerrit
Don't use any decoupling with the lab supply. Just connect it directly to the first stage instead of what you have.
If there's no low frequency rise, the decoupling is the problem.
What exactly is the decoupling circuit used? Seems like it must be well over 100k in series with the B+..
If there's no low frequency rise, the decoupling is the problem.
What exactly is the decoupling circuit used? Seems like it must be well over 100k in series with the B+..
Hi Rayma,
Right now there is no decoupling between the input triode and the phase inverter triode. Both are connected to the same power rail.
Regards, Gerrit
Right now there is no decoupling between the input triode and the phase inverter triode. Both are connected to the same power rail.
Regards, Gerrit
- Home
- Amplifiers
- Tubes / Valves
- 6SN7 input stage unexpected frequency response